紀由屋分享坊
Would you like to react to this message? Create an account in a few clicks or log in to continue.

公告:
紀由屋分享坊將於近日進行大規模更新,期間排版及貼文內容可能有所變動,敬請見諒。
kikyus.net will undergo a major update soon. During this period, changes in layout and post content may occur. Please bear with us.
生成工具:

herbertlawson
herbertlawson
屋友
Online
Offline

文章數 : 2
紀由幣 : 0
注冊日期 : 2023-12-30

Nepal plane crash caused by pilots mistakenly cutting power, says report Empty Nepal plane crash caused by pilots mistakenly cutting power, says report

周六 12月 30, 2023 12:48 am
Nepal plane crash caused by pilots mistakenly cutting power, says report

A plane crash in Nepal that killed 72 people, including two infants, was most probably the result of its pilots mistakenly cutting the power, said a report by government-appointed investigators.

This caused a loss of thrust that led to an "aerodynamic stall".

The Yeti Airlines flight was flying from the capital Kathmandu to the tourist town of Pokhara on 15 January.

It is the country's deadliest plane crash in 30 years.

The flight on 15 January, which involved an ATR 72, was the flight crew's third sector of the day, shuttling between Kathmandu and Pokhara.
https://www.taskade.com/p/01HJRN6ZD41295NAGYRV55WY8M
https://www.taskade.com/p/4-2-4king-2-hd-01HJRNWP3970ACAYG886EZRCHY
https://www.taskade.com/p/2023-hd-01HJRPZ5ZGAG3FHTW789DAYDR4
https://events.humanitix.com/host/suparer
https://events.humanitix.com/host/4king-2
https://events.humanitix.com/host/teeyodfull
https://events.humanitix.com/host/mansuang
https://www.taskade.com/p/01HJV22ZFTW0RVD5Y2XE2NYV3G
https://www.taskade.com/p/01HJV39ATANQ93C9PC37TCWRBD
https://events.humanitix.com/host/you-and-my-stars
https://gamma.app/public/2023-HD--fd4ogli4l50fuyc
https://gamma.app/public/HD--nwjy2ue9j8lm3rk
https://www.taskade.com/p/hd-01HJV4TH97GW3QZ8T94NWD1PXT
https://events.humanitix.com/host/mr-nice-guy-the-lonely-man

The privately owned plane crashed in the Seti river gorge just 1.5km (0.9 miles) from the airport, prompting a rescue operation that involved hundreds of Nepalese soldiers.

"Due to its momentum, the aircraft flew for up to 49 seconds before hitting the ground," aeronautical engineer Dipak Prasad Bastola, a member of the investigating panel, told Reuters.

The pilots had likely put the condition levers, which control power, in the feathering position instead of selecting the flap lever, he explained. Mr Bastola explained that this caused the engine to "run idle and not produce thrust".

"Following the un-intentional feathering of both engine propellers, the flight crew failed to identify the problem and take corrective actions despite the Crew Alerting Panel cautions," the report said.

The report also listed a lack of appropriate technical and skill based training, high workload and stress, and non-compliance with standard operating procedures as contributing factors to the accident.

It added that the aircraft had been properly maintained, had had no known defects and that the cockpit crew had been qualified in accordance with the rules and regulations of the Civil Aviation Authority of Nepal.

More than a dozen investigators from the US, Canada, France and Singapore were involved in the investigation.


查看下一個下一個上一篇主題查看上一個
這個論壇的權限:
無法 在這個版面回復文章